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FITTING ONBOARD |
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Land
Cruiser FJ43 with a Chev 350 V8 |
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The
York Compressor provides a better solution for compressor needs than the
eccentric vane type (Sanden Compressor) commonly found on most vehicles. The The For more information on the
http://www.ccicompressor.com/Features.aspx Service manual at: http://www.ccicompressor.com/docs/ccisect1.pdf |
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This
is the final work of art.
I
have not apportioned cost to the bracket, since it is made up of bits and
pieces. If you had to pay someone else it would be expensive, because it can be
time consuming. |
The
compressor was mounted, directly to the engine block and I had to manufacture
an adjustable idler pulley so that the belt could be tensioned. The existing
drive pulley from the engine crankshaft also had to be replaced and a used
one was obtained from Thundersport, |
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Later
I was offered a small filter that screwed onto the intake The
little black plastic filter can be seen here. Both
solutions are fine the one is just a little easier. |
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After some “sukkel” and a lot of effort, eventually the |
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Phase
2 - Compressed |
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In order to provide a reservoir of air to operate air tools and to
provide the big “whoosh” of air to seat a tubeless tire onto the rim, I
commenced with a section of 140 mm diameter schedule 40 seamless pipe. This
pipe is also known as steam pipe and is almost 6mm thick. Two brackets were welded
on which bolted directly to the chassis of the Cruiser. Holes were drilled in
the pipe, where ¼ inch BSP collars were then fitted and welded.
The cost of the schedule 40
pipe was about R350. In the picture alongside
the fitted air-tank can be seen, bolted to the chassis, in front of a square
rear bumper that I made which doubles as a water tank. |
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To fit all the fittings and
connections for the inlets and outlets, ¼ inch BSP threaded socket
connections were first turned down on the outside, so that a small collar
resulted. They were then inserted from the inside of the pipe and then welded
inside and outside. The reason for this is that
I do not want anything to pop out. The shoulder provides a natural restraint
to prevent any possibility of a blow out. |
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Three collared sockets were
welded on the inside of the second end cap which is the business end.
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The over-pressure valve
blows off air once it reaches 8- bar. Adjustable valves are
available as well as ones that will pop of at a higher pressure. 8 bar
inside the tank is however more than sufficient. When the air-tank is full,
there is sufficient volume to re-bead the Bruisers 33x12.5x15 tyres, without
having to start the compressor. The tap on the left of the
picture is the outlet for the bumper water tank. |
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On the inlet side, an air
hose routed from the compressor The air hose is rated at 10
Bar and should the pop-off valve malfunction, the next thing to blow before
the tank, would be the air hose. |
Currently the tank is
turned on with a switch mounted on the dashboard,
which is also connected to a light
which comes on. A safety cover is Failsafe should be the word
here and under the circumstances I believe that there are
enough safety measures built in to prevent the tank from over pressurizing. |
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The tyre inflator and
gauge, all fitted with quick-connect fittings Whilst the main purpose of having on-board air is
to have a large enough supply of air to reseat a tubeless tyre, additional
advantage is gained since you can now operate a variety of air-tools and
become almost self sufficient – at least whilst the engine is turning. The same arguments that are
however applicable to an electric winch vs. a mechanical or hydraulic winch
are applicable here. |
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(http://www.tooltime.co.za/ A mini-grinder, a drill and a ratchet were
the obvious choices. Besides small grinding
requirements you also need a tungsten carbide bit, which is the correct way
to clean a tear in a side wall before fitting a gaiter in the event of a tyre
being cut. |
I have also used the drill
on a number of occasions in the workshop, since it is compact and can get
into places that my big electric drill cannot. |
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The air tools work fine
albeit that they flatten the tank and every now and then I have to wait for
pressure to build up again. However, they do not
flatten the tank so rapidly that it becomes a hindrance to use them. Greater
volume would have been better but then a larger tank would have to be fitted
and somewhere compromises have to be made. |
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The marvels of the modern bushman? |
Similarly a tool oiler can also be used on any tool fro which oiling was
required and would connect in line according to requirement. |
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The real test for the
system and the air tools came some months later when I attended the Old
Trucks meet at Babanango. One of the “Old trucks” a
Jeep Gladiator turned off the bolts that attach the prop shaft to the gearbox
and required an “easy-out” to remove the broken studs. The offending broken bolt
was first ground flush with the dye grinder and then drilled with the
air-drill and removed. I might add that everyone was suitably impressed with
the installation and the fact that these tools were available and did their
job. |
What a luck having a mobile
workshop in the bush. |
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At the same time the air
duster came in very handy when I lost a filling on a tooth. The sharp edge was
in a very awkward position and caused my tongue to become very sensitive. Eben Henning mixed up some quick set Araldite, whilst I
blew the cavity dry with compressed air. My wife then did the patching of the
broken tooth. It worked and held till I got back to the dentist to sort the
filling out. The grinder also came in
very handy when I had to grind off the inner ring of a stuck bearing from a
trailer axle, when I stopped to assist a stranded boat owner, who had lost
his trailer wheel due to the bearing collapsing, next to the road. This, self acknowledged, mechanically inept
citizen was totally amazed, especially when I produced the right replacement
bearing from the “Tricky Green Bruiser’s” tool bin. If you need any help
contact me at boardman@mweb.co.za |